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Hew-Tex/Lone Ranger #1 SWD Drilling Report

  Lone Ranger #1 Well Tracking Chart.   HJ Daily Reports. 2019.12.18         Our RRC approved rate is 25,000 BPD @ max injection pressure of 6,000psiWe have finished our 20,000 Acid job and down our infectivity test and here are the results.Pumping Acid at a rate of 26 BPM or 37,440 BPD @ 1,600psiDisplacing Acid at a rate of 30 BPM or 43,200 BPD @ 2,000psi After allowing Acid to spend for 2 hours our Injection Test was conducted as follows:5 BPM or 7,200 BPD @ 95 psi10 BPM or 14,400 BPD @ 248 psi15 BPM or 21,600 BPD @ 450 psi20 BPM or 28,800 BPD @ 893 psi25 BPM or 36,000 BPD @ 1,485 psi30 BPM or 43,200 BPD @ 2,231 psi We have a very good SWD well and looks like we will have no problem going up to the 50,000 BPD rate as designed. Congratulations Folks!  2019.12.18         Standby.  Spot 4 single manifold and 2 lined frac tanks. Fill single manifold with2000 bbls FW. Cut mousehole 5′ in cellar and fab lid. Building cellar covers, pour ready mix cement in cellar to bottom of SOW. C/O blind flange on tree with 5 1/8″ 10M flange x 3″ 1502 with plug. PU trash on and surrounding location, load all misc items into trash trailer. Shut down for night. Petroplex Acidizing Company is rigging up on location making prep to Acidize well. 2019.12.17         Standby. Performed H5 test, witnessed by Field Inspector Steven Hayes of the TRRC.Installed piping, gauges, and needle valves on all casing valves. Dropped ball, allowed 37 minutes to fall, rupture pump out plug. Performed 2nd H5 test,...